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Harley 12-volt 65B generator rebuild
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The Model 65B, part number 29975-65B. The big oil-slinger washer on the gear means you have to tilt the end down to get the generator out of your bike. I prefer Channel-Locks on the gear rather than using an impact wrench. 1/2" wrench. This welded-up Chinese puller gets the gear off. Don't pry or use a slide hammer. Sometimes a claw puller will work, or even a battery post puller. I use anti-seize putting it back together, so it comes apart easier the next time. |
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Clean the end bell with solvent. The brush with solvent delivery works really well. Steel wool will clean really well. Make sure the bearing bore is clean and smooth. Another bin holds the parts as they come out of the parts solvent. The first bin stays dry, while this one goes to the sink. |
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The bush plate cleans up a little, but will also get a light bead blasting. The drive-side end bell gets cleaned out inside. Aqueous solvent is safer, but I prefer CRC Parts Solvent, its similar to the Safely-Kleen I saw in motorcycle shops. All these parts got the solvent treatment. |
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The "dry" bin with the frame, armature, and two brushes. Washing the solvent off. The end bell had gasket residue that did not scrub off. Be sure to wash out the bins. Get everything spotless, though the sealed bearings in the 65B keep out dirt. |
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The end bell after blasting with #10 beads.Blow off the parts, the tray, your body, and everything else so you don't track beads into your assembly area. I blasted the armature since I have never ever seen the lamination get beat into a spiral. This generator had a bolt missing. I have to think the armature was hitting the pole shoes and got beaten into this state. The astonishing thing is the generator still worked. You can see the diameter of the armature is smaller on the left side. Unlike the -65A generator, this armature comes with the bearings pressed on already. |
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The old armature (top) is obviously damaged, though it still made output. Bead blasting is not sand blasting. I did not clean some gasket material off, so I get it now. Mating surfaces, perfect. I like anti-seize to press in bearings and seals, while white lithium grease lubricates where the seal runs on the armature shaft. Bearings are sealed and pre-lubricated, at least I hope they are. |
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The seal just pressed in by hand. This might be too loose, maybe Yamabond 4 if the seal moves due to engine pressure. Both roll pins were sheared off the frame. I marked the position with a paint pen. The armature just slid into the end bell with hand pressure, good Japanese tight-tolerance precision machining. The lack of roll pins and one bolt might explain the damage to the armature. Same deal on the frame, I marked where the roll pin should be. Dykem also makes the red layout fluid everybody loves. |
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I built this generator tester decades ago. It uses a 115V DC motor to spin the generator. I used to use a rubber hose to connect the motor to the generator, but a YouTube comment made me realize I could braze a 1/4" drive 7/16" socket to an old gear, and file the shaft of the motor to to have a 1/4" square end. I drive the socket with two universal drives to allow for misalignment. It works great. While doing the job I often clean my hands with this pumice Fast Orange cleaner. Do watch out none of that pumice gets into what you are working on. I should wear gloves more, but I still prefer bare hands.I messed up my thumb fingerprint so bad it took 20 tries to unlock my phone. Time to see if I can turn that fingerprint reader off, I rarely use the phone. |
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